Tag Archives: smmb

First quadruped jump!

To demonstrate the dynamic capability of the full rotation quadruped, I figured I would start by doing some full machine jump tests to a relatively low height, just to show that it was capable.

Thus, I rigged up an open loop script which squatted a small fraction of the available distance, and then powered up at a relatively small fraction of the available maximum speed.  I don’t have the telemetry yet to extrapolate how high this will be able to go at maximum, but I think it should be a fair amount higher.  For now, I want to do some more instrumentation and walking testing (and have more spares) before I manage to break things by jumping really high.

First walking on the full rotation quad

Last time, I had finished physically assembling all the motors for the updated quadruped with legs that can rotate freely 360 degrees.  After the long summer break, I powered up and configured all the servos.  Then, after setting up the gait engine for the new configuration (for which there are still a TODOs when the lateral shoulder offset is non-trivial as in this configuration), I was able to achieve some amount of walking.  Here is one of the first videos I took, without much in the way of tuning or work.  The control is a little wobbly still, but so far there are no signs of any mechanical failures as with the older design.

 

Full rotation quadruped build continued

The next step in (re-)building the quadruped with a full rotation leg was getting all the motors ready.  I had to first install reinforcing rings on 6 of the motors:

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My epoxying station
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4x gearboxes with reinforcing rings installed

Then, I needed to lengthen the power leads on 3 of the motors to serve as the lower leg joint.

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Motors with longer power leads

Then I had to assemble all the new legs:

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Upper leg joints mounted
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Lower leg joints mounted
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All three remaining legs built

I mounted them all to the chassis:

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All the legs!

And then re-installed the battery stud and “resting” feet:

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Next up, will be actually powering them and getting it to walk!

Stripping the coaxial quadruped for parts

To switch to the full rotation gear design, I needed to get all my gearbox motors, some bearings, and a lot of other bits and pieces disassembled and ready for re-use.

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The remaining 3 non-broken legs from Maker Faire

Taking everything apart took a surprising amount of time, nearly a full day.  Each leg resulted in quite a collection of fasteners.  Seeing them all in one place made me realize how complex this has become!

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One leg’s worth of parts

I’ve also got the full set of parts printed for the full rotation legs:

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Now I just need to get to assembling and reworking to get them all installed!

First assembled full rotation leg

As I described earlier, the first draft brushless quadruped leg design was insufficiently robust for the gearbox driven motors and I am updating it to a geometry that allows full rotation.  I’ve made at least some progress on that front, so here is an intermediate report.

First, after doing some analysis, it appeared that the 3mm pitch 6mm wide belt was unlikely to be able to carry the full torque from the motors.  So I’ve switched to a 5mm pitch 15mm wide belt, which while still unable to carry the full torque indefinitely is only a factor of 2 or 3 off instead of a factor of 20 off.  Secondly, I added a bearing opposite the upper pulley so that it is supported from both sides.  The recommended belt tension for this belt works out to something like 120lb, which is a fair amount of cantilevering, even over the 16mm wide pulley.  The updated CAD looks like:

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And the newly added bearing can be seen in this section view:

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I did a first test print of all these parts and put them together.  While there were a few tweaks necessary for the second revision, it looks like this leg is probably usable.

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The shoulder and upper leg adapter installed, all the leg pieces splayed out
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Lower leg all assembled with belt and upper pulley installed
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All assembled!

Next up is building 3 more of them!

 

Full rotation leg design

Another of the failure modes observed during the 2019 Maker Faire was in my quickly slapped together leg design.  The shoulder joint was required to squeeze two motors together against a strongly tensioned belt, using nothing but a relatively thin section of printed plastic.  This caused it to deform, leading to belt tooth skipping, and then eventually to fail, leading to delamination of the shoulder joint.

My plan to resolve this is to switch to a leg design where the upper and lower leg are in series rather than opposing one another.  This is more like the Mini-Cheetah design from Ben Katz.  This has the benefit of getting the leg out to the side, so the upper leg is free to rotate 360 degrees, only limited by cable harnessing.  As seems to be my pattern, I’ll try making something out of 3d printed PETG first, optimize it some, and if I fail there, switch to metal.  Here’s a render of the current CAD:

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Eric from CireRobotics helpfully pointed out that I’m way over the design limit for the 6mm Gates belt I was using, so I’ll also be trying to bump up to a beefier belt in this iteration.

 

Working around motor shroud failures

As seen at Mech Warfare 2019, the existing gearbox motor shroud isn’t really up to the task of supporting the weight of a 20lb robot.  While I work on a more comprehensive redesign, I’ve got a short term fix in the form of another 3D print.  This is just a simple reinforcing ring, printed at 3mm thick, with the layer lines oriented so that layer separation will not be the primary failure mode.  It is attached to the outer housing via a thin layer of epoxy.

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The two halves of the reinforcing ring

Due to the unconventional orientation, removing support was a pain, but doable.

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A reinforced motor

Results from Maker Faire 2019

After a concerted push, I managed to get Super Mega Microbot “Junior” walking, for all of 15 minutes, then packed it up and went off to compete in Maker Faire.  Needless to say, with that much testing, I wasn’t expecting stellar results, and I wasn’t disappointed.  However, I did learn a lot.  Here’s some of the things that went wrong:

Gimbal and Turret EMI

For this new revision of SMMB, I updated the gimbal board to use RS485 and support the 5S system voltage.  I tested it some, but apparently not enough.  While I observed no problems during Thursday or Friday’s testing at the site, during the first Saturday match, after firing the gun a few times, the gimbal went into a fault state and stopped applying power.  The control scheme for SMMB relies on the turret being operational, so this not only made it impossible to aim, but also made it nearly impossible to drive.

I did manage to connect to the turret manually after the match to diagnose the problem, and discovered that the IMU had stopped communicating over I2C.  I had some half-baked logic to try and recover from that, but it was broken, and the only effective way to recover was to power cycle the whole unit.

Unfortunately, my matches on Saturday were all close together, so I didn’t have enough time to prepare a fix in between.  Thus, each match I got one or two shots off, and then the machine as a whole became effectively inoperable.

Likely, something in the new board, either in the layout or the decoupling capacitors, results in worse electrical noise than the old one when the AEG is fired.  This shouldn’t be too hard to resolve, either through tweaking the layout, or perhaps moving the AEG control to an entirely separate board.

Walking and Leg Robustness

When I got the gearbox system walking for the first time, I quickly noticed that one or more of the timing belts connecting the lower legs to their motor had a propensity to skip a tooth.  Since there is no position sensing directly on the lower leg, when that occurs the gait logic just has the incorrect position, causing the robot to fall over pretty soon afterwards.  I had never observed any tooth skipping in my previous direct drive leg, even when jumping for over an hour.  The first difference I thought which might be causing the problem was the lower pulley print, which I had initially done at 0.15mm but in the gearbox revision it was at 0.2mm.  So I printed a full set at 0.15mm, and swapped them in.  However, that didn’t fix it and I didn’t have any more time for mechanical solutions, so I tried to work around it by tuning the gait to be as gentle as possible.

Unfortunately, I wasn’t really able to come up with a gait that both could effectively move on the foam mat in the arena, and not occasionally result in belt skips.  Also, as I went along, the skips got worse and worse.  I tried upping the tension on the belt, lowering the tension on the belt, walking with a straighter leg and more bent leg, nothing much made a difference.

Finally, before my third match, I did more examining and realized that the shoulder joint was deforming significantly under the tension of the belt, resulting in the timing belt only contacting maybe half the pulley or less, and the rest dangling off.  Also, the pulley was out of alignment, so the belt was probably only effectively making contact in an even smaller patch.  Unfortunately, there was very little I could do about that aside from hope for the best.  As it turns out, that problem, while limiting the gaits I could use significantly, didn’t result in ending my run.

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Shoulder failure

Gearbox Outer Housing Strength

The entire gearbox effort was undertaken somewhat at the last minute, and with little thought to analysis or design for structural integrity.  At best, I made a gut check of “that’ll probably work”, and at worst, I gave it no thought at all.

It was an instance of the latter that caused the final and fatal failure in SMMBJ at Maker Faire.  In the gearbox chassis design, the lateral servos themselves support the entire weight of the robot.  Those gearbox servos transmit the entire load from the front plate of the servo, through the outer housing, then to the back plate, and finally to the chassis itself.  The problem in this case is that the outer housing is a 1.5mm thick (or rather thin) PETG shroud printed with layer lines perpendicular to the primary load.

On reflection then it was not too surprising that a 20lb robot walking around was enough to cause a motor’s shroud to separate at the layer lines, which is what ended SMMBJs run.  I had a spare motor and could have replaced it, however, it would likely have failed shortly afterwards too, and the shoulder was about to rip itself apart due to the leg tension problems mentioned above.  Thus I turned it into a “static display” and switched to a “show and tell” mode for the rest of the event.

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Crippled SMMBJ

Award

Despite those problems, the kind organizers at RTeam awarded me the “Most Innovative” award for trying to push the limits!

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Fixing the problems

Clearly, all of these issues can be fixed in a variety of ways, both easy and hard.  Keep coming to see my attempts!

Mech Warfare 2019 – First look

Well, Mech Warfare at Maker Faire 2019 has come and gone.  Maker Faire was a really awe inspiring event, and RTeam did an excellent job organizing the Mech Warfare competition.  There were something like 13 teams with moderately functioning mechs who competed across the 3 days.

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Super Mega Microbot “Junior”

My entry, Super Mega Microbot Junior, did manage to walk a bit in 3 matches, but had a previously unseen failure in the turret system that rendered it inoperable a short while into each match.  At the end of the 3rd match, one of the leg joints sheared off, and some other of the 3D printed parts were about to fail as well, so I declared it unrepairable at that point.

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In the arena pre-failure

I’ll write up a more detailed lessons learned and link to the videos of my matches when they get posted.  The videos aren’t all that interesting, given that I only scored perhaps 2 hits across all 3 matches. 😉

Walking and Maker Faire!

Alert!  I’m at Maker Faire Bay Area all weekend in the Mech Warfare area in Zone 2 (May 17-19, 2019 for you time travelers from the future).  Drop by and say hi!

If you were left in suspense last time, yes, the robot can walk!  Getting it to do so in a minimal way was relatively painless.  What I found, which hadn’t happened in earlier iterations, is that many types of dynamic motions would cause the lower leg belts to jump a tooth.  Needless to say, this was nearly universally fatal, as there is no direct position sensing of the lower leg.  This robot is heavy enough that my simulacrum 3d-printed timing belt pulleys just don’t cut it.

Well, there wasn’t enough time to actually get better pulleys now, so I just tuned the walking to be slow and gentle enough that nothing went awry.  Here’s the first bit of a 13 minute video I took of it walking around and shooting targets.

Now, that that was over with, I had a few minor things to finish up before heading out to Maker Faire.  I made some covers for the motors to keep BBs out.

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And I made a bracket so that I could attach the front and rear target panels to shoulder joints:

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And here’s a glamour shot of the whole thing in fighting form!

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Now that it was all ready, time to take it all back apart and pack it for shipping.

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And off to the airport I went!